Firebird2XC
Well-Known Member
Found this rummaging around on the net. Good job to the crew.
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An American Eagle Aerospatiale ATR-72-500, registration N494AE performing flight MQ-4756 from Midland,TX to Dallas Ft. Worth,TX (USA) with 41 passengers and 4 crew, was in level flight with the autopilot engaged, when the crew noticed a pitch mistrim message, disconnected the autopilot and found both control columns restricted in their fore and aft movements with a maximum movement of about one inch foreward and one inch backward. The crew attempted the jammed elevator checklist procedure twice, but was unable to uncouple the elevators (break the link between the two control columns). After slowing to 180 KIAS the crew found better control of the elevator. When the airplane lined up for the final approach, the elevator again seemed to have jammed. The crew went around and conducted a second, shallow approach to a safe touch down. While taxiing to the gate the elevators became unjammed and the crew regained full control of the elevators.
The NTSB released their preliminary report stating, that maintenance personnel found the brackets holding the left hand elevator down limit stop had fractured and separated from the elevator, so that the down limit stop restricted the movement of the left hand elevator.
The cockpit voice and flight data recorder were secured, several damaged parts in the area of the left hand stabilizer area and the left elevator were removed for further investigation. The NTSB concluded: "The rest of the airplane was released to the operator."
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An American Eagle Aerospatiale ATR-72-500, registration N494AE performing flight MQ-4756 from Midland,TX to Dallas Ft. Worth,TX (USA) with 41 passengers and 4 crew, was in level flight with the autopilot engaged, when the crew noticed a pitch mistrim message, disconnected the autopilot and found both control columns restricted in their fore and aft movements with a maximum movement of about one inch foreward and one inch backward. The crew attempted the jammed elevator checklist procedure twice, but was unable to uncouple the elevators (break the link between the two control columns). After slowing to 180 KIAS the crew found better control of the elevator. When the airplane lined up for the final approach, the elevator again seemed to have jammed. The crew went around and conducted a second, shallow approach to a safe touch down. While taxiing to the gate the elevators became unjammed and the crew regained full control of the elevators.
The NTSB released their preliminary report stating, that maintenance personnel found the brackets holding the left hand elevator down limit stop had fractured and separated from the elevator, so that the down limit stop restricted the movement of the left hand elevator.
The cockpit voice and flight data recorder were secured, several damaged parts in the area of the left hand stabilizer area and the left elevator were removed for further investigation. The NTSB concluded: "The rest of the airplane was released to the operator."