Minuteman
I HAVE STRONG OPINIONS ABOUT AUTOMOTIVE LIGHTING!
“The investigation determined the aircraft’s nose landing gear did not retract properly due to hydraulic fluid contaminated with water freezing. After running multiple checklists and a conference call with engineers, the pilot’s attempts to center the nose landing gear failed. During those attempts, ice formed inside the main landing gear struts, and they did not fully extend causing all valid Weight on Wheels sensors to indicate the aircraft was on the ground. The aircraft transitioned to “on ground” flight control law, despite being airborne, and became uncontrollable. The pilot successfully ejected, and emergency responders were at the scene within a minute.”